You signed in with another tab or window. Reload to refresh your session.You signed out in another tab or window. Reload to refresh your session.You switched accounts on another tab or window. Reload to refresh your session.Dismiss alert
When I run yarprobotinterface, the robot does not calibrate the l_knee.
Detailed context
Below, the error:
[ERROR] from BOARD 10.0.1.8 (left_leg-eb8-j0_3) time=154s 378m 40u : MC: overheating. Temperature hardware limit exceeded. The motor has been turned off to prevent it from being damaged by overheating. (Joint=l_knee (NIB=3), Raw_temperature_value=385)
Btw, using the motor GUI, I'm able to calibrate the l_knee, so everything seems fine. Also touching the motor, it doesn't seem hot, so I think it's a fake overheating.
Additional context
No response
How does it affect you?
No response
The text was updated successfully, but these errors were encountered:
ciao, scoverizzato la coscia SX e trovo il filo rosso staccato dalla TDB del ginocchio.
dopo aver risaldato il filo @isorrentino fa il test e la calibrazione va a buon fine.
Rimontato le cover.
Robot Name π€
ergoCub 1.1 S/N:001
Request/Failure description
When I run
yarprobotinterface
, the robot does not calibrate thel_knee
.Detailed context
Below, the error:
[ERROR] from BOARD 10.0.1.8 (left_leg-eb8-j0_3) time=154s 378m 40u : MC: overheating. Temperature hardware limit exceeded. The motor has been turned off to prevent it from being damaged by overheating. (Joint=l_knee (NIB=3), Raw_temperature_value=385)
Btw, using the motor GUI, I'm able to calibrate the
l_knee
, so everything seems fine. Also touching the motor, it doesn't seem hot, so I think it's a fake overheating.Additional context
No response
How does it affect you?
No response
The text was updated successfully, but these errors were encountered: