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iCubGenova09 (iRonCub3) S/N:000 β Right shoulder pitch cable has one broken wire #1684
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We will attempt a quick fix if we borrow the tools! |
Here's the type of connector and size (AWG): |
With @pillai-s we crimped the broken cable! We started the robot and joint works as expected! The fix is temporary because the repaired wire is shorter than the others. Also no glue is applied on connector. In general the whole cable seems short so probably if a new crimping is necessary we might need to replace it! |
cc @Gandoo |
ciao @gabrielenava ho ripristinato il cavo e preparato i cavi spare |
grazie mille @Gandoo! |
Robot Name π€
iCubGenova09 (iRonCub3) S/N:000
Request/Failure description
We just saw that the cable that connects the optical encoder to the right shoulder motor
E1
that has one wire broken.Detailed context
The broken wire is the black one. We do not recall any activity that caused this issue.
The glue seems old and hardened.
Additional context
How does it affect you?
It may block iRonCub experiments.
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